Effectiveness of the Desulfurization of Coke-Oven Gas at PAO Magnitogorskii Metallurgicheskii Kombinat


如何引用文章

全文:

开放存取 开放存取
受限制的访问 ##reader.subscriptionAccessGranted##
受限制的访问 订阅存取

详细

To assess the capabilities of the desulfurization system for coke-oven gas in coking-product recovery shop 2 at PAO Magnitogorskii Metallurgicheskii Kombinat (MMK), the effectiveness of all stages in sulfur recovery unit (SRU) at the shop is analyzed. It is found that the capacity for catalytic conversion of hydrogen sulfide to sulfur is not being fully utilized. Its use would raise the temperature of both stages in the SRU’s R-6201 Claus reactor. The optimum temperature of the second catalytic stage of the R-6201/2 unit and maximum conversion to sulfur cannot be achieved because of the insufficient heat-exchanger efficiency resulting from surface deposits of sulfur. Observations at waste-heat boiler 1 of the elemental-sulfur production department in the copper plant of Norilsk Nickel’s Transpolar Division show that sulfur condensation on the heatexchanger surface decreases the heat transfer in the waste-heat boiler by 20–40%. Modification of the heating system for the second stage of the R-6201 Claus reactor in coking-product recovery shop 2 at PAO MMK by introducing a regulated bypass line is proposed.

作者简介

O. Platonov

Koks i Khimiya

编辑信件的主要联系方式.
Email: oipla@yandex.ru
俄罗斯联邦, Moscow

补充文件

附件文件
动作
1. JATS XML

版权所有 © Allerton Press, Inc., 2018